I’m definitely getting into the fun part of the project. I spent part of the evening trying to add a servo to the front holo projector. It was a little more tricky than I thought it was going to be. I’d seen photos and vaguely remember a setup on one of the tables at C4, but until tonight I didn’t understood the nuances of the angles and forces need to move something with a servo, so it was frustrating and fun at the same time.
Most people seem to use the same basic method to move pie panels, doors, holo projectors etc. And that’s to convert servo rotation into a linear movement using a push rod attached to the servo horn.
I’d bought some random mini servos from Tower Hobbies a while ago (Hi-Tec HS-55), and a push rod/linkage assembly from ebay. Problem was the servo was too small to fit the rod attachments. I managed to improvise and this is what I finally came up with
Please ignore the kinks in the rod, it really should be straight, but I’d tried to copy what I’d seen at C4 and got it totally wrong
If I was to do this again I’d probably skip the pre-made assemble and make something in acrylic and parts from the local hardware store.
I also created a short video to summaries and demo the new setup.
As I explain in the video it’s not perfect, and I need to affix the servo more permantely to the dome rather than using velcro and I’m not entirely confident the linkage to the back of the HP will last very long.
The good news the Hi-Tec servo is definitely powerful enough to move the HP and will probably work for the pie panels as well.
I also need to decide if I’m going to add some code to my micro-controller to automate random movement.
I replaced the failed Pittman dome motor last night, and thought I’d post some pictures of the failed gearbox.
The pen tip is pointing to the failed gear in the center of the picture. The teeth are almost stripped flat.
And this is the new motor opened up and how the gearbox should look. Again the gear in question is in the center of the shot. Notice the teeth!
I’m not confident that it will not fail again, and I may need to look at an alternative. I’m hoping the issue was my failed attempt to use batting tape to line the dome bearing to help with traction, but the gear may have been slowly failing with the constant harsh stop/starts on such a small gear. I know of at least one other builder that had a Pittman dome motor fail in the exact same spot.
I finally got a chance to fully test out my slip ring last night with some servos.
I first had to finish soldering up my little boards that would handle signal routing and power.
Rather than try and explain in words and pictures how the setup works I made this short video to try and give a good overview and show the slip ring in action.
I still need to make little brackets to secure the D sockets to the boards, and decide the best place to locate them in Artoo.
I stripped my first set of gears in a motor this weekend. I was goofing around on the driveway showing Artoo to some neighbors across the street when suddenly the dome stopped working. I heard this really bad crunching noise then a very quiet motor spinning.
I quickly pulled him into the workshop and the dome off to see what was up.
A couple of months ago I had lined the inside track of my dome bearing with some batting tape to help the dome wheel grip. It had been slipping and the resulting noise was very annoying. The tape seemed to be the perfect solution …… until the gearbox failed.
I think what had happened was I’d left R2 sitting in the van all day and when I finally unloaded him the glue on the tape had heated up and when I started to spin the dome it balled up - jamming the wheel and breaking the gearbox.
Gerard had a similar failure trying to fix the squeaky slipping wheel. He’d over tightened the tension spring which stopped the dome the moment the motor stopped - but again this put extra pressure on the gears in the Pittman motor causing them to fail.
I started work on my test slip ring tonight and hope to get it installed in the next few days and report back on a new group order.
The sample slip ring has eighteen 2A circuits and I plan on grouping together 6 or 8 for the +/- 12VDC uplink to the dome, leaving ten circuits for PWM/servo signals. To save on circuits I’m not planning on routing the +/- 5VDC from each of the PWM pairs through the slip ring. As a result each RC channel will require just one wire allocated on the slip ring. I’ll just tap of the 12VDC in the dome and re-create a separate 5VDC supply for the servos.
Out of the box the slip ring wires are loose and really needed protecting.
I bought some braided expandable nylon wire wrap from a local surplus electronics store for less than a dollar.
I wrapped the ends in electrical tape to hold things in place.
Now that I have the wire wrap in place I can start soldering the wires to the connectors.
Here’s an overview video on how I plan to implement the wiring
Here’s something else I’d forgotten I’d worked on before C4 and not posted.
The original dome periscope had a small raised lip around the side ports/windows. Neither my PVC or aluminum periscope kit has this so I improvised.
I used a 1″ Nylon gasket from the plumbing department at my local Ace Hardware store, and just superglued it in place. However, paint has a real hard time adhering to Nylon, so if I was to do this again I’d probably try and find an O ring made from something different. Also if you try and rough up it up you’ll get fine strands that will never go away.
I guess I’m posting this as an idea rather than a solution.